Revolights are a very cool product that illuminates the front and rear wheels on a bicycle. The only problem for me is the cost; around $220 is a little too expensive, although they are worth it if you can afford it. I decided to try and make a set of wheel lights for my road bike using SMD LEDs. A few months ago I got the bright idea to make use of some LEDs that I had laying around. Designing a quick board and sending it over to Laen’s PCB service got me 30 or so boards for a small cost. The boards were originally going to be used for lighting the inside of my 3D printer; but after all the work of soldering SMD LEDS and wiring everything together, I reused a scanner backlight that output more evenly. Since the LEDs were already wired, all I needed to do was attach the lights and batteries with cable ties everything for the initial testing. Two identical LiPo batteries for a small RC helicopter were used to power the lights on each wheel. A small switch soldered by the battery acts as a ON/OFF switch. The first version seems to work fairly well, although it is not waterproof, the next version will be. I would also like to include a microcontroller to do some extra light
It seems like as soon as I fix something around the house, something else breaks. The furnace decided to stop working recently and I didn’t realize it until I woke up the next morning. I decided to see if I could fix it seeing as I replaced the hot-surface ignitor the year before. After watching the start-up of the furnace, I could see the ignitor was lighting the gas, but would go out shortly after leaving the blower running. After doing some research I figured it could be some oxidation build-up on the flame-sensor, giving the control board a false reading. I removed the sensor and cleaned it with a green scouring pad until it appeared clean. After replacing the sensor, the furnace seemed to work again and heated the house to the correct temperature. About a day later I noticed the furnace had started to have the same problem again. This time it seemed the flame would never light, even with the ignitor glowing hot. Again I took to the internet for more information on how furnaces function. Inside they seem pretty simple; a control board, gas valve, ignitor, blower & inducer motors, and various sensors.
After finding a flow diagram on the internet I began to try and troubleshoot the problem. After a few hours I gave up and decided to call a repairman the next day (it was like 3am at this point). The repair guy came, tested a few things and concluded it was the furnace control board; he said it would be around $300 to replace. Knowing I could replace the board myself, I declined the service and just paid for a diagnostic fee, $49. Next I called a friend who was able to get me a new control board for $79 right down the street from my house; all within 30 minutes of the repair guy leaving my house.
I began by first removing the old control board from the furnace. Taking pictures allowed me to quickly record the orientation of the various wires attached to the old board. Once everything was unplugged, I removed the old board from the furnace and set it too the side. The new board looked to be of much better quality then the old one, and also had status LED’s, which the old one did not. Once everything was replaced and reconnected I started the furnace up again….it did the same thing.
This time the board flashed the LED with an error code saying the pressure switch was malfunctioning. I couldn’t get a new switch locally, so I called the another repair place since the first guy was wrong anyway. After seeing what kind of switch it was, he located one nearby and had it installed in an hour for $100. In the end I didn’t really need the control board, but it was nice having the status LED and I learned quite a bit about how a small gas furnace operates.
A few weeks ago while looking for a better motor for Liam’s go kart, I came across these electric dirtbikes on some forum. The idea of an electric dirtbike in my neighborhood seemed like a good plan. I have always wanted to get a dirtbike or enduro-style bike to ride around on. Two stroke bikes are loud and would annoy the neighbors really fast. With a little more research I found that a used Razor MX500 would be a cheap initial investment to get into the world of electric bikes. One weekend of searching craigslist allowed me to pick up (3) MX500′s for $175.
The first bike I picked up worked but the freewheel on the back was shot so the motor could not engage the back wheel. This freewheel seems to be the problem with the Razor dirtbikes. A new freewheel was like $12 from some scooter site. While waiting for it to arrive I decided to use the MIG to weld the freewheel solid. It might not be the best solution but it allowed me to be able to ride the bike for a quick test.
After the first test my first impressions were that the bike was kinda slow. Being that it was made for a rider less then 170lbs and I weigh 165lbs, I figured the bike was made for a smaller person. So we rolled the bike back into the garage and let it charge completely over night. The next morning I decided to try it before work, not thinking anything would be different. After a full charge the bike took off pretty fast, and reached a decent top speed. I need to check my max speed, but it definitively surprised me with its power and speed. The bike feels like an under-powered pit bike.
While searching for the first bike, I replied to a couple of different adds on craigslist. The first bike I got for $100 from some kid about 15mins away. He wanted $150 but asked if he would take $100 because I thought I would have to buy a new rear wheel; overall the bike was in decent condition. The second two bikes I got from one person way out by Eureka for $75. These bikes were a little rough with surface rust but looked like to good a deal to pass up. The add asked for $150 because only one of the bikes worked. Later he sent me an email saying he couldn’t get either running and would take $75 for the pair, so I agreed. We picked both bikes up and brought them back to the garage to see what was wrong. One bike just had a faulty brake cable that wouldn’t let the motor engage. Once the cable was fixed that bike worked fine. The batteries and the freewheel was also shot on the second bike. I also noticed later that the chain was also missing.
This whole time I was already researching how to make it more powerful. Various people have done extreme things to these little bikes. Stock the MX500 runs at 36V with a 500watt motor. I tried adding one battery from the second set of bikes to the first to make it 48V. It ran faster but I returned to 36V in fear of ruining the different sets of batteries. I really wasn’t too concerned about speed as I was the torque. The 500watt motor really did not have that much acceleration. I decided to try finding a bigger rear sprocket first instead of new batteries, motor, controller, etc. Currie makes a 90 tooth sprocket that would have to be modified for use on the MX500. Someone posted on a forum to have one custom cut for the bike. A company out of Ketucky, Rebel Gears custom cuts aluminum sprockets. So after a few calls I had a 95t and 100t sprocket on order for the MX500. It took almost two weeks but in the meantime I worked on modding the frame.
First I decided to cut the top battery tower support.
Then a flat piece of steel was welded to the rectangular tube.
Then the whole piece was welded to make it look like top battery tray was just extended.
I also began to weld extra steel rod around the back for looks. They still need more grinding to make them look better; I have only had the MIG welder for a few months.
I also decide to chop the handlebars and use and old MTB bar welded in place.
After all of the welding the rear sprockets finally arrived. After rigging some chain together the sprocket went together easily.
Below is a comparison with the new 100t on bottom and the stock rear sprocket on top. Its quite a bit bigger.
Here a few more pictures of the bike at its current state.
I the future I would like to get the frame powdered coated; I am not really of fan of the red. Tried painting the plastics with Krylon’s Fusion paint. I need to do a few more light coats, but it seems to work ok.
Next comes the 48V setup…….
Here are some pictures of the go-kart I built for Liam.
A little off-topic…but these boys are fuckin nutz!
Laen’s PCB Order comes through again with some nice quality boards for a recent design. I wanted to try soldering a few TQFP microcontrollers in a toaster oven, and ended up using a 16F877A. Using the 16F877A allowed enough pins to connect quite a few devices together. Since you get three copies of any PCB that you order, I decided to try and use one for building a scoring controller for an airhockey table.
My basic requirements for the board were:
- ICSP port
- LCD character display
- 7-segment display using a MAX7219 driver IC
- Thermocouple support using a MAX6675 sensor IC
- Piezo speaker
- 2 onboard buttons for input
- 4 onboard LED’s
- RS232 I/O via software -> PICBASIC
- Unused pins brought out to header pins
I then went to work using eagleCAD for the schematic and board layout. After many changes I finally settled on a design.
The design was then sent off to Laens PCB order for fabrication. A few weeks later the boards arrived and I began to assemble them. I decided to assemble just one in the beginning to see if they were even going to work.
Here was the build log:
PIC16F877A TQFP Development Board ver.1 Log
ver1 of the development board has a few traces that were not fully routed during design.
Pins E.0 and E.2 need to be connected via jumpers.
The LCD_AnyPin.pbp must be used to allow different pins for the LCD.
The MAX6675 silkscreen is upside down, turn the IC 180 before placement.
The silkscreen by the speaker shows D.6 while it is actually D.7.
The Thermocouple I have is WHT=+, RED=-
After soldering the minimum required components, my first attempt at programming via ICSP did not work. The ICSP connector must be placed a certain way; see completed board. Finaly I was able to successfully program the 16F877A via the ICSP, although a program to flash the LED failed.
A simple PICBASIC program to flash the LED connected to E.0 initally would not work. I tried various settings of the fuses but nothing seemed to work. While looking over the board layout trying to figure out the problem, I noticed two traces form the onboard LEDs were not fully connected to the PIC! I dont know how this slipped through, but was an easy fix with some small gauge jumper wire. I then decided to remove the 33pF capacitors on the 20mHZ crystal and replace them with 22pF. I also changed the 47uF capacitor on the 7805 with 10uF. After reprogramming the 16F877A again, the green LED began to blink! Now I was finally starting to think the board wasn’t a complete bust. I soldered on the final components and decided to wait until tomorrow to try it.
I did not want to start the board without configuring the 16F877A to use the various I/O’s first. My initial test of the MAX7219 did not work. I also noticed the MAX6675 was now becoming very hot. I removed the MAX6675 until I have more time to look at it in detail. Initial thoughts are wrong routing of signals. I finally got the MAX7219 to work. After moving the code over from the PID program I noticed there is a subroutine “Transfer” that directly calls the PORTS instead of using a variable. Once both were changed to their corresponding ports the 7segment display jumped to life! The MAX6675 still wasn’t working properly.
I finally figured out the cause of the overheating MAX6675. The artwork that was silkscreened on the PCB has the chip orientation wrong. Once I noticed this I de-soldered the old chip and placed a new one using the reversed orientation. This fixed the MAX6675 and now works perfectly. After using the LCD_AnyPin.pbp from Darrel Taylor, I then was able to set the individual pins for the LCD bypassing PICBASICs restrictive settings. So up to this point it seems everything is working that I have tested. I need to check out the RS232 connection and the onboard speaker.
The onboard speaker works after noticing the silkscreen is incorrect by displaying port D.6 while it is actually D.7.
Everything seems to be funtioning on the second board I built. I used SMD LED’s instead of thru-hole. The SMDs I had can be soldered nicely between the pads for the thru-hole versions. The finished board looks much nicer than when using the SMD LED’s. While building the second board I had trouble getting it to reliably start. It seemed intermitent at best with no reason. Later I narrowed it down to either the crystal or the trim capacitors near it. Once the trim capactitors were removed The board seemed to work perfectly. I read something a while back that mentioned the capactince? of the entire board can allow use of no trim capacitors. Whats weird is the first prototype has the capactitors and works fine.
Here are some images of the assembly process:
PCB just after coming out of the oven
After installing basic components to allow use of the ICSP
Completed development board with LCD removed
Picture of the bottom side showing the wire jumper fix
Completed board w/LCD attached running a demo
Running a test of the MAX7219 7segment driver
Using PICBASIC, I created a demo for the board testing various features including the LEDs, speaker, thermocouple, and the 7segment display. Ill post the code in another post. Right now I am trying to implement a simple menu system for selecting various tests.
Final thoughts on the project: I was impressed the board had only a few mistakes that were fixable; especially for not testing the design first via simulation or using a breadboard.
The MAX6675 pcbs I had manufactured finally got populated. These will be used in conjunction with a master station running PID control software. The boards were created with EAGLE Light. This is the first time I have ordered a pcb that I had designed in EAGLE. I didn’t have time to build a prototype first, so I just ordered them anyway. I used Laens PCB Oder for the boards. They were reasonably priced and you get (3) copies of each board that you order. The board has (4) MAX6675 chips with decoupling capacitors for each. Each 6675 has a 2-pin screw terminal for attaching the thermocouple. The MAX6675 uses onboard cold-junction compensation, and is located in close proximity to each screw terminal. The chips are controlled via the I²C bus and share CLK and DATA pins while being selected with individual CS pins. Everything is brought out to a 8-pin SIP connector that I can plug into a breadboard or connect into a larger master unit.
Here is the EAGLE layout of v1:
Here is the datasheet for the MAX6675.
I’ll post some PICBASIC code eventually that shows it in use with a 7-segment display using another board I had ordered at the same time.